Sticks McGee
Well-known member
So today on my break I ran home and got my home compressor. I have a truck I need to put some tires on and I figured this might prove to be a good experiment. Here are the details:
Compressor A.
My shop compressor. A large ingersol (80 gallon, two stage running on 460 v)
This compressor is set at shut off to have 160 psi. I used my hose reel that is attached fairly close to it. The hose reel is probably about 15 years old and it is 3/8" hose and it is 150' long. I drained the compressor down a bit and let it run to cut off.
Compressor B.
Craftsman oiless 33 gal compressor. It's rated at 1.6 hp and 5.1 cfm at 90 psi.
I did a modification to it where I put a T fitting right near the outlet. The outlet on this is 1/4" NPT. originally the fitting came out to a T. one side of the T was the pop off valve and the other side was stepped down to a tiny hose that ran back up to the regulator manifold, thru the manifold and to the supplied two quick couplers. My modification takes the shortest path I could get right to my quick coupler bypassing the regulator manifold and the regulators. All fittings are 1/4" NPT and my hoses are 3/8" with 1/4" NPT on each end. So in short I have 33 gallons of 150 psi air available to the hose, then to the tool.
Impacts.
My 1/2" IR 2131 and the shops IR 2141 3/4" impact. Each impact has a 30" whip hose attached. Both of these impacts in is excess of 10 years old.
Lugs.
Wheels are 19.5" unilug 33mm nuts. These wheels I always torque with my 3/4" torque wrench to 485 ft.lb
With both compressors fully ramped at 160 psi (shop) and 150 psi (home) I connected the 3/4 impact to the craftsman. I pulled 4 nuts off with no struggle whatsoever and just started on the 5th one when the compressor kicked on. This is a 33 gallon oiless compressor connected to two 50' 3/8" airlines to make 100 ft of line running thru 1/4" NPT fittings running an older 3/4" impact. The lugs have been on a while so I am not sure what the breakaway torque is to break them loose. The 3/4 did not even struggle to spin them off. After the compressor kicked on I switched over to the hose connected to the shop air and did a couple with that. The impact performance was seemingly identical.
My point here is I am not trying to say that an expensive compressor isn't better. I would love to have a 60-80 gal 2 stage myself. I guess my real point is that the average DYI doing brakes on his/her car or truck should not have a problem running a 1/2" impact and getting the lugs off and on. Most people who are DYI at home are not gonna be running an air hungry 3/4" impact and pullng off 33 mm nuts that torque at 485 ft. lb
When I first fired up my home compressor after my wife bought it for me for christmas, the way it was ranning thru the tiny fittings was choking it down to a point where it did not work worth a piss. I also run hi flo fittings on all my stuff and have been doing that for years at work. When I got the compressor at home I decided to use the same fittings.
Compressor A.
My shop compressor. A large ingersol (80 gallon, two stage running on 460 v)
This compressor is set at shut off to have 160 psi. I used my hose reel that is attached fairly close to it. The hose reel is probably about 15 years old and it is 3/8" hose and it is 150' long. I drained the compressor down a bit and let it run to cut off.
Compressor B.
Craftsman oiless 33 gal compressor. It's rated at 1.6 hp and 5.1 cfm at 90 psi.
I did a modification to it where I put a T fitting right near the outlet. The outlet on this is 1/4" NPT. originally the fitting came out to a T. one side of the T was the pop off valve and the other side was stepped down to a tiny hose that ran back up to the regulator manifold, thru the manifold and to the supplied two quick couplers. My modification takes the shortest path I could get right to my quick coupler bypassing the regulator manifold and the regulators. All fittings are 1/4" NPT and my hoses are 3/8" with 1/4" NPT on each end. So in short I have 33 gallons of 150 psi air available to the hose, then to the tool.
Impacts.
My 1/2" IR 2131 and the shops IR 2141 3/4" impact. Each impact has a 30" whip hose attached. Both of these impacts in is excess of 10 years old.
Lugs.
Wheels are 19.5" unilug 33mm nuts. These wheels I always torque with my 3/4" torque wrench to 485 ft.lb
With both compressors fully ramped at 160 psi (shop) and 150 psi (home) I connected the 3/4 impact to the craftsman. I pulled 4 nuts off with no struggle whatsoever and just started on the 5th one when the compressor kicked on. This is a 33 gallon oiless compressor connected to two 50' 3/8" airlines to make 100 ft of line running thru 1/4" NPT fittings running an older 3/4" impact. The lugs have been on a while so I am not sure what the breakaway torque is to break them loose. The 3/4 did not even struggle to spin them off. After the compressor kicked on I switched over to the hose connected to the shop air and did a couple with that. The impact performance was seemingly identical.
My point here is I am not trying to say that an expensive compressor isn't better. I would love to have a 60-80 gal 2 stage myself. I guess my real point is that the average DYI doing brakes on his/her car or truck should not have a problem running a 1/2" impact and getting the lugs off and on. Most people who are DYI at home are not gonna be running an air hungry 3/4" impact and pullng off 33 mm nuts that torque at 485 ft. lb
When I first fired up my home compressor after my wife bought it for me for christmas, the way it was ranning thru the tiny fittings was choking it down to a point where it did not work worth a piss. I also run hi flo fittings on all my stuff and have been doing that for years at work. When I got the compressor at home I decided to use the same fittings.