How could I have forgot about the 4010? What a pain in the ***! If you go back a few pages and go back to about August/September you’ll see where we left off on that.
I was trying to rebuild the selective control valve. Then dad ended up buying a second used one to add on to it. We that turned out to be a nightmare.

I started rebuilding the couplers as well as the valves. I’d never worked on a set a valves, especially, not one of these old style sets. I couldn’t get things set to where the were supposed to go.
I had some issues with a few parts. Replaced some parts. Replaced all the seals and o-rings. Things were just a pain. The adjustment was all over the place. But then it came time to get things ready for fall so that job just had to sit.

Things were busy....

I had a few chances between things to try and readjust the valves but I just could never get them right.
Fall finally wrapped up. I was catching up on other things. It was time to finish this thing.

I thought I had things where the needed to be and put things together.

Valves were mounted, oil lines in place, couplers mounted, linkage connected. It was ready. Then two of the oil lines blew immediately.

So I had to have some hoses made. Got those on and tried things out.

I hooked up a cylinder to test them out. NOPE! The valves still weren’t right. So by this point I’d ran out of patience and had too much else to do. So I took them to the dealer.
That called for more parts, plus the time for the time l take apart, reassemble and adjust everything. That was a hefty bill...it took over two weeks to get them back to as that fell around New Years.
Got them on and there were finally good to go. But there was another thing dad wanted to do while it was in the shop.

The plate that side under the fuel tank also covers up the hydraulic pump. Which sits in front of the radiator. At some point in time someone apparently needed to remove the hydraulic pump. Their answer to the problem was to just torch out a hole to remove the pump. You wouldn’t think it but this giant hole then allows a lot more dirt to enter the radiator.

So that job meant removing the radiator, fuel tank, lines, hoses, air filter, shields, etc. Which also meant a major cleaning job on the front end. It looked like it hadn’t been touched in years. Definitely wasn’t taken apart when someone gave the tractor a paint job. But that also meant while we were there we may as replace some things. So that meant radiator hoses, hydraulic pump drive bushings, fan belt, fuel line, hydraulic steering line, the plate itself which caused this whole mess, and a few other hoses.

There were some other jobs to take care of in the midst of this so it wasn’t able to be finished all at once. But eventually things started going back together.

So. One evening dad, Noah and myself got with and and finished putting everything together. I had Noah cleaned everything up. Last thing to do was fill the radiator. I thought it looked rough before I had Noah wash it. Afterward I was a bit nervous. The radiator looked in worse shape than I’d thought. Sure enough! The damn thing started leaking coolant right away!
This happened on a Friday. There is only one guy in the area that still rebuilds radiators and he’s about to retire. Come Monday we dropped it off to him. He checked it. It was going to need a new core. Now this happened during the cold, snowy spell we had. Took him a day to look at it. He ordered a core. The core came from Texas. Took a week to get here. He put it in. It leaked worse than the one we had! So he sent it back. That timed out when Texas was shut down due to the winter weather. So that set things back. Then the guy hurt his hand doing something and that set him back. It took 3 weeks to get this damn radiator back!

Finally on March 2 I got the radiator back and got it on the tractor.

The next day on the 3rd it was finally going and out of the shop! Finally! This thing had been sitting in the same spot since late July. That’s a long time.
So after many headaches. Many issues.
Lots of money. Lots of waiting on parts to arrive. It was finally running and done. It’s still not 100%. There’s some more I’d like to do to it. But it’s ready to go. It’ll likely get feed grinding and auger time this year. But at least it’s going better than it was.