Here we go...extricated some photos...I'm going to guess this was 2006 or 7.
Aligning the two forklifts so I could remove the cylinder...can't tell you how it was done exactly, there are many warnings in the manuals not to get your hands or arms crushed or pinched when the carriage goes free of the chains. Use clamps and wood blocks. There's enough weight there to cleanly snip off a body part so pay attention.
So I used sawhorses, plywood, and black plastic to keep oil from soaking thru. Slightly in conflict with above recollection without the benefit of pictures
Disassembly of parts, trying to keep everything in order.
The old U-cup seals were all cracked just like this. Still functioning with some weepage but it was a near-max lift that really got them leaking as I recall.
Originally I had these green colored seals. I think OEM Clark. And I damaged a couple of them with my initial installation plan. So I was hoping I could get individual seals from Hercules Bulldog (now its Hercules). They told me they had an entire kit with a "premium material" cup and so I ended up buying the entire kit from Hercules. I had to buy it thru Motion Industries as a pass-through since H-B would only sell to an entity with an industrial account.
The rings that are pictured there are very important, read-on. The U-cup has something like a quad ring pushed inside the center of the "U" and so its very stiff in the radial direction. This has to bypass a set of internal threads for the endcap, while compressed, to avoid damage. My solution was the rings, some are metal, some are steel banding material, and some are PVC. I was in full experimentation mode. But I would now try to go with the PVC since its cheap and easily machined.
The procedure is basically this. Slip the ID of the cup over the OD of the inner rod. Then using pliers and substantial clean hydraulic oil, gently compress the seal inside the comperssion-ring. Its a fight for it to want to spit back out, hence the vise grips.
So now the seal is fully compressed inside the ring. Same as the smooth bore as its about to go into.
Generously lube and slide the whole assembly forward until it bottoms out. The ring is protecting the seal from the sharp threads.
Now using a flat rod, tap the seal in, working around the circumference, until it leaves the plastic ring and enters the smooth bore. Once seated, its ready for the end cap to be installed.
Same concept with steel band material. This worked but was a lot more time involved to get the correct length of band, bronze-braze it together, smooth all of the edges with a file, and finally test fit it to make sure it cleared the internal threads. It was fully deformed due to the stresses in the joint until the now-compressed seal forces it round. The alternative is trying to machine a thin ring, which has its own challenges. Maybe someone with a 3D printer could create one to-size on the first try with minimum effort
I had the carriage completely off. A little crusty.
Refreshed as well as grease cutting cleaner could get it.
I put on new side shift hoses, the old ones were cracked where they rolled over the sheaves, from the Parker store, nice and flexible. These are not super high pressure.
Its been all good ever since
