Finished out the PCV/CCV system. Baffle installed on right valve cover under the suction fitting.
Exhaust crossover as CCV suction port was a failure. Plugged and moved on. Why? The two small holes on the bottom of the crossover aerated the oil badly. I believe there is a continuous film of oil splashed onto the bottom of the intake, feeding the two holes. Small holes make high velocity. To do again, more larger holes, or something else.
Added a restrictor to the inlet side of the CCV. Turned down a Holley jet OD to fit ID of 6AN. Slightly smaller than the restrictor at the manifold.
I had ordered a cheap, $25 catch can/separator before I had replumbed and resolved the oil issue. Since rings are new decided to go ahead and use it, see what it captures. Made another clamp type mounting bracket.
Tucked the canister back on firewall behind the brake booster. It is plumbed in-line with valve cover inlet and the manifold.
With oil contamination issue resolved, the truck runs so much better. I think at low RPM there was a mis-fire due to oily plugs and oily mixture that wouldn't light. Now with some clean miles the carburetor has fixed itself. Different AFR behavior. Glad I stopped trying to 'tune' the inconsistent behavior, was never going to get there. $2000 in EFI would mask the issue somewhat, but not solve. The lean tip-in is mostly gone once warmed up, and the overly-rich conditions are reduced.
The carb tune isn't perfect, or as good as it was before the heads and cam, but it's OK, drivable now. It fires immediately and idles smoothly stone cold, with no choke. It struggles a bit in gear cold, but the high idle takes care of that. Hit the switch and all is well, can drive off without waiting. Leaving the high idle on does negatively effect tip in, as the transfer slots are too far exposed and fuel circuit feeding them is being consumed already. Not a big deal though, once rolling the inertia removes need for high idle.
After months of work the motor is finally running like it should, and I can enjoy the results. I pulled the motor July 12th, and had it running again beginning of September. Then almost two months of chasing my tail on carb issues and carb tuning for an oil issue. Some self-inflicted just trying to make things custom and complicated. I'm glad I didn't run it completely out of oil, or trust the false dipstick readings. I was probably 1.5 qts low when I changed the oil and added the equalizer tube.
So now I can move on to other things. Going to see if it tolerates 87 octane fuel with 35* total timing. Not sure it needs 35 but no pinging now with 89. Can also revisit accelerator pump tuning. Try #1 cam screw position. Maybe epoxy the nozzle and go down to 0.031. WOT is mid 12s fairly consistently so I think that is good enough. Have an odd jet split, 72/65. The motor seems to start to roll over at 5200 RPM, which is as expected.