With the DSX fuel system in place I resumed tuning and verified it resolved my issue. I continued tuning only to have the car suddenly start running extremely rough in the middle of a WOT pull. There was plenty of fuel, the tune was actually a bit rich but the car was shaking like crazy with the check engine light flashing. I pulled into the nearest parking lot and scanned the codes and there were over 10.
I limped the car home and began doing research. Initially I assumed something went wrong electronically since I had just added the DSX kit but I eventually had my wife turn the engine over while I had the valve covers off and I saw the intake valve for cylinder 4 was not moving at all. Interestingly the car did not identify a dead miss for cylinder 4 which is something even a c5 can do. I initially believed I could just pull the passenger side head and replace the failed DOD lifter until I took off the valley cover and could clearly see the lobe on the cam was destroyed. Everything I read said you have to pull the engine to replace the cam so out it came.
I had been aggressively working to pay the car off, and only had about $3,000 left. I began looking into various options to fix it and none of them were cheap so I decided I wanted to push the car in to the back of the shop pay it off and then save up money to do a cam / DOD delete, and forged pistons.
I was pretty frustrated with the situation and aside from the lifter failure (which I do not believe I was at fault for) the car needed the dash pad replaced along with the radio. Both are common issues (dash common for 3LT cars due to leather shrinking.) The car had been a money pit from the beginning pushing timelines back for everything else (cars, shop, house) and I decided I'd see if I could just sell it as is.
In the end someone drove up with a trailer from Kentucky and took my problems away. With the proceeds I was able to pay off my truck and for the first time 8 years I had no car payment!
He ended up messaging me a couple months later after having done everything I planned on doing along with the LT4 injectors/pump and made ~750whp. I hope it treats him better.
Now I could turn my attention onto the shop again.
-Hillrod