Dad and I did a slab-dash job of moving the phase converter outside and built a little roof for it, and the noise level is tremendously more tolerable. I've been pretty busy the last little bit:
I made some home-made levelers to level the two new lathes to save $250 over buying them from McMaster. (Just days before a friend of dad's told him that he had tons of those, *sigh*.) I copied the design from holdfortheengineering on instagram. They consist of a piece of 5/8" all thread with a 118 degree point on the end and just just sit in a drill point dimple on the pad. I used the lagun for some of the machining.
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Dad likes his lathes up pretty high so it's up on blocks. Unfortunately the through holes are inboard as well. It looks very tippy being up so high, but I would have to body-slam it just to get it to shake in the slightest. No forklifts in this shop, and not an earthquake prone area so I'm really worried about it. If the scenario was different I would do it differently.
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Dad took the feedbox apart the other day and couldn't find anything wrong, so he put it back together and the feed works in all positions now. Nice! So here's how it looking right now (the feed rods and stuff got polished up after this picture)
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It's very close to being right. The electrical is 100% working right, the gearbox is good, apron is good, TS is good, coolant works, etc. I called recently and asked for a quote on the gib, headstock shaft, and some way wipers. Lagun records aren't too great, they keep having to ask questions about which version it is because apparently their records don't reflect the small changes. It's an 82 model btw.
We've been using it a bit now too, having the fixed feed. I made a shim and a new stud so that we can run our AXA toolpost for the time being.
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Now that I understand the gearbox it's really not that bad. The one thing that I really, really, really like about it is that the metric thread settings can be set with the only the face-panel levers. No change gears required! I single pointed my first ever metric thread the other day. That is a really nice feature I've needed for a long time. It does have a change gear, but it's only needed for cutting worms, which I have yet to ever need to do.
I turned two boring bar blanks, a 1" and a 1.5", which I'll probably setup for 3/8" tooling.
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I was trying to align the tailstock while cutting them and I never could get it totally consistent. Pre-leveling, dad was complaining about a lot of taper is his work, which I attributed to the lack of leveling or just dad's machining skills. He's right that there was something more going on though. The headstock was way out of line! I made a light cut on a 3" piece that was plenty stiff enough for zero deflection and it tapered 6+ thousands over those 3 inches. So we got that aligned this week. It's not perfect, it runs 1/2 thou over 4 inches, then jumps up to 1 at 6". But it's a lot better!
Dad also discovered that the Lagun has a brake. We knew it had a foot-pedal but didn't see any cable or brake so we just assumed it was a foot switch. Turns out the input pulley is also a tiny drum brake. I made some adapters and we hooked it up with a bicycle brake cable. Works good.

Another item off the list.