James_B
Well-known member
It's been a while since we moved from Newfoundland to Nova Scotia, and one of the tools that I haven't had time or space to set up was my Universal Laser Systems VLS 4.60 LASER cutter/engraver.
In Newfoundland, it was easy. When it was delivered, it was unloaded from the truck and went straight into the garage. I just unpacked it, bolted on the legs, fitted the casters, and rolled it into a corner of the garage.
To give you an idea of size, the engraver is 36" wide, 36" deep, stands 39" tall, and weighs around 270 lbs.
Before winter arrived, I mounted a baseboard heater on the wall behind the laser cabinet as the LASER tube life expectancy between rebuilds is reduced if the o-ring seals get too cold.
Here's what the interchangeable LASER assembly looks like. They're avilable in power output levels from 10 to 75 watts. The 10 to 30 watt models are smaller and will fit into a desktop size engraver, but the bigger tubes need to go into what ULS refers to as a Platform LASER.
Inside my LASER assembly is an air cooled 50 watt (minimum) carbon dioxide LASER tube, and the larger units (like mine) have a high 4 figure price tag.
A necessary part of the installation is some sort of air extraction system that will flow at least 250 cfm and will maintain 6 inches of vacuum in the cabinet. Smaller units can use an charcoal filtered extraction system, but it's far cheaper to use an off the shelf "dust collection" style blower that's ducted outside. In my case I had a 650 cfm extraction blower that connected via flexible ducting to a vent I mounted in a panel of the garage door.
Other than the cold, the only problem I had with it set up in the garage was the one time I managed to get dust on the optics while doing carpentry work for the house renovation ... and when the LASER was next fired up, that dust caused a $600 failure of the penny sized final focus lens. Something that I don't plan to repeat.
The only other failure I've experienced is the failure of a tiny magnet in the "door interlock" switches. An identical replacement magnet assembly cost me less than $4.
After 3 years of use, it was all packed back in its crate for the move to Nova Scotia.
In Newfoundland, it was easy. When it was delivered, it was unloaded from the truck and went straight into the garage. I just unpacked it, bolted on the legs, fitted the casters, and rolled it into a corner of the garage.
To give you an idea of size, the engraver is 36" wide, 36" deep, stands 39" tall, and weighs around 270 lbs.
Before winter arrived, I mounted a baseboard heater on the wall behind the laser cabinet as the LASER tube life expectancy between rebuilds is reduced if the o-ring seals get too cold.
Here's what the interchangeable LASER assembly looks like. They're avilable in power output levels from 10 to 75 watts. The 10 to 30 watt models are smaller and will fit into a desktop size engraver, but the bigger tubes need to go into what ULS refers to as a Platform LASER.
Inside my LASER assembly is an air cooled 50 watt (minimum) carbon dioxide LASER tube, and the larger units (like mine) have a high 4 figure price tag.
A necessary part of the installation is some sort of air extraction system that will flow at least 250 cfm and will maintain 6 inches of vacuum in the cabinet. Smaller units can use an charcoal filtered extraction system, but it's far cheaper to use an off the shelf "dust collection" style blower that's ducted outside. In my case I had a 650 cfm extraction blower that connected via flexible ducting to a vent I mounted in a panel of the garage door.
Other than the cold, the only problem I had with it set up in the garage was the one time I managed to get dust on the optics while doing carpentry work for the house renovation ... and when the LASER was next fired up, that dust caused a $600 failure of the penny sized final focus lens. Something that I don't plan to repeat.
The only other failure I've experienced is the failure of a tiny magnet in the "door interlock" switches. An identical replacement magnet assembly cost me less than $4.
After 3 years of use, it was all packed back in its crate for the move to Nova Scotia.
