Dear GJ Vise friends,
Here is a new thread about vise handles. Most vise handles have either a steel ball or formed ends to keep the handle attached to the vise. This thread will offer one way to replace a “formed end” vise handle. I am not a blacksmith and there is probably a better way to do this but … here is what I am doing.
Photo 1 - I picked up this Desmond Stephens 41S Simplex Steel Slide vise from CL last summer. It has had a hard life!! I should name this vise “school of hard knocks” since I am going to learn a lot fixing up this vise. It will not be easy like the Chas Parker I just did.
Photo 2 - The handle was totally wasted. At first I thought I could straighten it so I heated it and began to work on it. I was able to get it 80% good but the main screw kept getting in the way. So… I fixed that problem.
Photo 3 – I ground off the formed end of one side of the handle so I could work on the handle alone.
Photo 4 – More heated straightening effort.
Photo 5 – I got the handle about 95% straight. At this point I am starting to feel good about it so I began to polish up the handle. After polishing, it still looked terrible. You can’t see it in the photo but the whole handle looks like a beaver was chewing on it. It had gouges and nicks along the whole length.
Decision time, I decided to scrap the handle and make a new one. Almost all vises have 5/8 or ¾ diameter handles. This vise has a 9/16 diameter handle. Maybe that’s why it is all bent up. I struck out finding 9/16 round bar stock locally, so I went fishing for donor material. I found a jack handle that was 9/16 and I was just ready to cut it up and I thought hmmm… where did this come from and why is it in my garage?? I decided not to cut it up. I did have some 5/8 diameter stock on hand so I am going to use that. This will require increasing the hole in the main screw.
Photo 6 - The existing hole for the handle was19/32 (1/32" over the 9/16 handle) so I ran a 19/32 drill thru the whole to set it up for re drilling. With the 19/32 drill inserted in the main screw, I clamped it all to the drill press. not shown is the C clamp holding the drill vise to the table. I redrilled with tap magic
Photo 7 - I opened up the hole to 1/32 over 5/8 using a 4 flute hole enlarging drill. The 4 flute works best for this application.
I am at my 7 photo limit so I will post the other half of this procedure later.
Take Care,
Greg
Here is a new thread about vise handles. Most vise handles have either a steel ball or formed ends to keep the handle attached to the vise. This thread will offer one way to replace a “formed end” vise handle. I am not a blacksmith and there is probably a better way to do this but … here is what I am doing.
Photo 1 - I picked up this Desmond Stephens 41S Simplex Steel Slide vise from CL last summer. It has had a hard life!! I should name this vise “school of hard knocks” since I am going to learn a lot fixing up this vise. It will not be easy like the Chas Parker I just did.
Photo 2 - The handle was totally wasted. At first I thought I could straighten it so I heated it and began to work on it. I was able to get it 80% good but the main screw kept getting in the way. So… I fixed that problem.
Photo 3 – I ground off the formed end of one side of the handle so I could work on the handle alone.
Photo 4 – More heated straightening effort.
Photo 5 – I got the handle about 95% straight. At this point I am starting to feel good about it so I began to polish up the handle. After polishing, it still looked terrible. You can’t see it in the photo but the whole handle looks like a beaver was chewing on it. It had gouges and nicks along the whole length.
Decision time, I decided to scrap the handle and make a new one. Almost all vises have 5/8 or ¾ diameter handles. This vise has a 9/16 diameter handle. Maybe that’s why it is all bent up. I struck out finding 9/16 round bar stock locally, so I went fishing for donor material. I found a jack handle that was 9/16 and I was just ready to cut it up and I thought hmmm… where did this come from and why is it in my garage?? I decided not to cut it up. I did have some 5/8 diameter stock on hand so I am going to use that. This will require increasing the hole in the main screw.
Photo 6 - The existing hole for the handle was19/32 (1/32" over the 9/16 handle) so I ran a 19/32 drill thru the whole to set it up for re drilling. With the 19/32 drill inserted in the main screw, I clamped it all to the drill press. not shown is the C clamp holding the drill vise to the table. I redrilled with tap magic
Photo 7 - I opened up the hole to 1/32 over 5/8 using a 4 flute hole enlarging drill. The 4 flute works best for this application.
I am at my 7 photo limit so I will post the other half of this procedure later.
Take Care,
Greg