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Between 265 & 485 SQ/FT Made By Miller Studios

Workspaces sized between 265 and 485 squarefeet.
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MadeByMiller

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I’m really happy with my Einscan scanner.
Good to hear! I likely won't be going straight to a scanner at the caliber of the HX, but the Einstar I think would be a good entry level scanner for me. Most of what I would scan likely would be small items in the desktop configuration anyway. I wonder if all of the Einscan tools use the same software?
 
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slodat

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I bought the reverse engineering bundle. It included Geomagic Essentials. It’s a very slim version of Design X. Design X makes scan to parametric models fast. It’s also $20k per seat. So, Geomagic Essentials it is for me! Not sure if they have a similar bundle for their new Einstar. Einscan’s software works and I don’t have any issues with it.

I definitely recommend Vision Miner should you decide to buy.
 

OutlawDrifter

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Anyone here have any Case 1816 experience to share?

Not first hand, but CASE makes a good machine, and have been doing it for a very long time. I have a personal bias against them as I don't like hand controls for the bucket/mast...I grew up with foot controls on older Bobcat machines. I don't like the new ISO joysticks either...I'm just set in my ways and crotchety like that :ROFLMAO:

So with that...I think it will make a great machine for you, and looks like its been well cared for! Those little machines are a nice size and easy to move.
 
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MadeByMiller

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Nice. If I had it to do all over again, I think I would have looked for and bought a used skidsteer or small loader when we moved to use in the yard and then sold it after the yard was done. Moving all that dirt around by hand with a wheelbarrow was a PITA.
Thanks Mike! I definitely have plans for utilizing this machine for yard work/landscaping around the property. I also have a pretty large gravel driveway so it will perpetually be used for dressing that up as well. It's easy to see the usefulness/utility of a small skid loader around the property, even just for lifting or loading/unloading heavy stuff (700 lb lifting capacity).

Maybe you (or anyone reading this) can help or confirm a couple of known issues with the machine. The most glaring problem occurs when you get into higher rpm's - anything above about half throttle there is seemingly a misfire that is severe enough that the whole machine shakes. The solution from what I have seen in my research is likely new, properly set points and condenser, do you agree based on that information? I should add that it's powered by a single cylinder gas 16hp Kohler (I believe a K341).

The second problem is not one I experienced in my test run, but was shared to me by the previous owner: the engine will sputter out and die after 30-45 minutes of run time. After allowing the engine to cool for 15 minutes it will fire up and run as normal. I believe this is due to the 12v aftermarket fuel pump being mounted too close to the engine in an area without airflow, causing a vapor lock phenomenon. If that's a proper diagnosis, it should be as simple as relocating the fuel pump.
 

OutlawDrifter

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Maybe you (or anyone reading this) can help or confirm a couple of known issues with the machine. The most glaring problem occurs when you get into higher rpm's - anything above about half throttle there is seemingly a misfire that is severe enough that the whole machine shakes. The solution from what I have seen in my research is likely new, properly set points and condenser, do you agree based on that information? I should add that it's powered by a single cylinder gas 16hp Kohler (I believe a K341).

The second problem is not one I experienced in my test run, but was shared to me by the previous owner: the engine will sputter out and die after 30-45 minutes of run time. After allowing the engine to cool for 15 minutes it will fire up and run as normal. I believe this is due to the 12v aftermarket fuel pump being mounted too close to the engine in an area without airflow, causing a vapor lock phenomenon. If that's a proper diagnosis, it should be as simple as relocating the fuel pump.

I would definitely give the ignition components a look in regards to the first issue.

2nd issue is common with gas powered units, this is generally fixed with an electric pump swap. Keep in mind, these pumps push better than they pull. I always wired mine up with relays to keep them with full 12v power. The pump may be dyind due to the heat as well.
 
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MadeByMiller

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Not first hand, but CASE makes a good machine, and have been doing it for a very long time. I have a personal bias against them as I don't like hand controls for the bucket/mast...I grew up with foot controls on older Bobcat machines. I don't like the new ISO joysticks either...I'm just set in my ways and crotchety like that :ROFLMAO:

So with that...I think it will make a great machine for you, and looks like its been well cared for! Those little machines are a nice size and easy to move.
Thank you for your input!

I actually quite like the controls. I have thousands of hours of seat time in newer Caterpillar skid loaders with the joystick controls and I think they're awesome! I have no Bobcat control experience, but I am turned off by the idea of having to use hands/feet, maybe because I'm not very coordinated ha.

Little is right, less than 1900lbs dry!
 
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MadeByMiller

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I would definitely give the ignition components a look in regards to the first issue.

2nd issue is common with gas powered units, this is generally fixed with an electric pump swap. Keep in mind, these pumps push better than they pull. I always wired mine up with relays to keep them with full 12v power. The pump may be dyind due to the heat as well.
Thank you Marc! Glad to hear that I may be on the right track with the diagnoses.
 
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MadeByMiller

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Thats a pretty clean machine. It looks pretty old but someone took care of it.
It's an original 1816, some call it the 1816A as it's the predecessor to the 1816B and 1816C, so it was built between '73-'77. It's tight mechanically, but looks a bit nicer in photos than up close as the man who sold it to the previous owner applied a slightly sloppy brush on paint job. It's not perfect, but it's presentable from a distance which I like since I have no indoor parking space for it, so the neighbors will at least not have to look at a beat up machine.

It's really begging for a couple of arms. Like this.
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Haha, your next scratch build??
 
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MadeByMiller

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Delivery came this morning of our Case 1816! I had worked into the deal for the seller to deliver the machine the hour drive to it's new home as I don't have a trailer. Due to the two issues I mentioned earlier I don't plan to do any actual work with the machine until I complete the tune up (parts are on the way). It didn't stop me from busting out the fancy camera for a bit of a photoshoot though!
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The previous owner told me that the gentleman he'd purchased it from had installed the 16hp Kohler K341 (1973 manufacture date), new tires, and applied the paint job and decals. I wish I could track down the exact year of the machine based off the serial number (9825372) but I can't find a resource for decoding anywhere. As you can see, the "bucket" is pretty rough and rusted through in spots. I put bucket in quotes because it's actually not originally a bucket at all, it was a manure fork that has had a bottom and sides bolted on. Fortunately, I believe I have tracked down an original bucket and even a set of the factory option wide wheels on the other side of the state.

Thanks for looking!
 
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MadeByMiller

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This past weekend I dove headfirst into overhauling the engine on our Case 1816 skid loader. It ended up being a bit more of an undertaking than I anticipated, but overall the process went smoothly without incident and was very rewarding. As a reminder, the machine was running quite rough when brought past about half throttle - I set out to fix this issue.

Pulling the engine was pretty straightforward. First I disconnected the battery and pulled the seat off, giving me access to the hydraulic pump mounting bolts. The pumps, being belt driven off the crankshaft of the engine, have a slotted mounting hole to pivot the pump and add belt tension. Simply loosening the mounting bolts on all three hydraulic pumps released the tension on the belts, but due to little (or zero, more on this later) clearance between the crank pulley and the bulkhead of the machine, the belts can only be removed by unbolting and pulling the engine rearward. I disconnected the two hydraulic oil lines that run to the cooler mounted on the engine compartment gate so I could swing it out of the way, then fuel, exhaust, and electrical were disconnected, engine unbolted, and finally divorced from the machine. Kohler K341 engines weigh about 125lbs, but fortunately I was able to muscle it out of the engine bay and on to my workbench without hurting myself.

I apologize for the crappy cell phone photos, I didn't have the bandwidth to pull out the fancy camera during this project.
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Although quite clean as is, I opted to degrease the engine, engine compartment, and the hydraulic compartment underneath the seat at this stage. I used Dawn dish soap in my foam cannon to cut through the grease and oil which worked fantastic to thoroughly suds up the offending areas prior to hand scrubbing with various brushes and following behind with the pressure washer to blast the junk away. The result was pretty satisfying and revealed just how nice this machine is underneath it all.
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I next focused my attention on cleaning up the edges of the engine mounting plate that had been haphazardly torch cut and welded roughly in situ by the man who did the engine swap. In the act of removing the engine I almost sliced my hand open about 100 times, but a cutoff wheel, files, and DA sander made pretty short work of squaring up and trimming the lackluster handiwork of aforementioned man.
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To round out the work on the engine compartment, I decided to take the time to roughly mask off and paint the engine compartment to help with leak detection in the future and protect the bare metal surfaces. When I went to town to engage in the wild goose chase that is parts sourcing, I foolishly forgot to bring a small part with me for paint matching purposes. Referencing photos from my phone to help choose a color was less than accurate as is apparent in the following photos. Despite Cub Cadet Yellow by Majic (sold at Tractor Supply) not being a good color match for the more modern Orange-ish Case color the machine was painted with at some point, I think It's actually pretty close to what would have been the original Case Industrial Yellow, and with the engine in and the gate shut it's pretty well hidden. One whole can and too many heavy coats later:
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That wraps up the engine compartment refresh, next up we'll take a look at the engine...
 
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MadeByMiller

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As I've mentioned a few times now, at some point the original 16hp Tecumseh powerplant was replaced by a 16hp Kohler K341 manufactured in 1973. It was easy to find parts for this engine and I ordered them mostly through eBay along with an original Kohler service manual from the origin year of the machine. Here you can see them all laid out, gaskets (cheaper to buy the full set than individually what I needed), ignition components (coil, points, condenser, spark plug, plug wire), and a factory replacement fuel pump.
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I brought the engine to the necessary state of disassembly and inspected what appears to be a healthy half-century old piece of built to last American iron.
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The head had my attention next. I scraped and cleaned the carbon using a plastic razor blade and half a can of brake cleaner before inspecting it for flatness on my granite surface plate. The callout for flatness said that a .003" feeler gauge should not fit between the mating surface and surface plate, and it passed that. Regardless, I could feel a slight rock and noticed some discoloration in the corner near the exhaust valve that to my untrained eye could have been a source of compression leak, so I lapped the head by sticking some 1000 grit sandpaper to my surface plate with soapy water and sanding in alternating patterns. You can see that the corner where the exhaust valve sits is still lower than the rest of the mating surface, but I was confident that it was close enough and not worth sanding out. The before and after is fun to look at:
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Meanwhile, some of the grossest (but glitter free!) oil I've ever seen was slowly draining as I began to clean up the block/piston/valves/intake. The cylinder walls were clean and scar free and I'm confident that this engine has more than enough life left in it for my service needs.
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Not pictured, but I also removed the valve cover and inspected/reset the clearance between the valve stems and tappets. I tightened the adjustable tappets a couple of thousandths to bring them into the tight side of spec. I then installed and set the new points to the appropriate .020" gap specified in the detailed Kohler service manual. Next I fastened the head back to the block with new headgasket and grade 8 bolts torqued to 30 ft-lbs in sequence. To wrap up the engine parts install, I reinstalled the practically new carburetor, new coil, condenser, and replaced the wire feeding the points from the coil.

We're almost ready to stick this sucker back in place now.
 
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MadeByMiller

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Here's where we left off, fully reassembled and ready for fresh oil after draining as much of the old junk as possible overnight.
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If you remember, I mentioned in the original overhaul post that there was "zero" clearance between the front of the crank pully and the bulkhead plate of the machine. That was caused by this abomination of a cobbled together, farmer welded triple pulley setup. In order to somewhat align the hydraulic pump pulleys to the crankshaft setup, the front pulley had to be pushed really far forward. This, combined with the predictable runout of the crank pulley, was causing a self clearancing scenario between the pulley and bulkhead, as shown here:
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Certainly not ideal. The proper fix would be to fab up a new and proper crank pulley, but due to time constraints I decided to cheat and shave off approximately .09375" from the face of the pulley. I achieved this by rotating the engine with a cordless drill on the flywheel nut while sanding the face with an angle grinder, deburring with files when I was satisfied with the amount removed. The result after a spray bomb rebuild is at least functional and now the crank pulley and bulkhead are at a safe distance from one another.
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At this point, it was finally time to prepare for a reunion of engine and machine. No photos of this, you'll have to use your imagination as I did my best to remain patient with a project that was taking me longer than anticipated. The unelaborate engine wiring harness was leaving some to be desired in terms of routing and protection, so I remedied that with some nice braided loom and zip ties in the hydraulic compartment, routing the wires more directly to their source of termination in a safe, easy to access fashion. This cleaned up the engine bay more than I was expecting and left me with my final task, which was installing the new fuel pump and reconfiguring the fuel lines.

The pump mounted nicely in the stock holes in the lower left side of the engine compartment, but rather than leave the mess of excess fuel hose and hook it up as it was, I brought it to a state that my obsession could comply with. This meant placing the fuel shutoff valve behind the main fuel filter instead of the old position in front of the filter which made no sense to my mind. I also relocated the main filter and shutoff to the hydraulic compartment underneath the seat instead of crowding up right next to the engine with about 14" of excessive hose.

With the fuel and electrical system reconfigured, I wrestled the old Kohler back home into the spruced up engine bay, slipping the belts on the dieted crank pulley and fastening it to the plate I had cleaned up earlier. Electricity and fuel was supplied to the big red heart, and after reconnecting the battery I was ready to test out my work. Key inserted, I anxiously switched the ignition on. A proper clickety-clackety greeted me from the new fuel pump, and after a few seconds of priming the fuel system, I turned the key to the start position. I cranked for a few seconds with no signs of combustion. For a brief moment I cursed myself for what I was sure was some stupid mistake that would require hours more work on an already overschedule project, but skeptically I hit the key again. This time the un-muffled engine roared to life - success! I walked around the back of the machine watching for leaks and anything out of the ordinary, thankfully finding nothing. The true test was now to see if I could push the throttle to max RPM and maintain a smooth running machine or if all of this work had been for nothing. Once again - success! I thought anyway, it was tough to discern how smooth it was running without re installing the muffler. So I did just that, threw the muffler back on and started the engine back up. Indeed, my inclination of success once the exhaust decibels were toned down to a reasonable level was verified, so I then operated the hydraulics with no seat installed to verify that the hydraulic pump belts were tensioned sufficiently and not slipping. With that confirmed, I tossed the seat back in to properly make a test run, as both of my sons excitedly climbed into my lap to join me as the sun was setting over a fulfilling project's evening.

The test run resulted in a satisfying increase in power and functionality over the pre-overhaul machine status. Not a slight increase either as predictably, the ability to rev the engine out to full throttle effectively made the experience of operating a completely different machine. Feeling a healthy sense of accomplishment and exhaustion, I parked the 1816 for the night.
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In conclusion, I can't be certain which variable or combination of variables was causing the misfire condition, but I'm glad to have it up to 100% now. I learned that as I've gotten older, more experienced, and my patience level raised, projects just go smoother. It really brings the enjoyment and reward out when you can bring a project to the finish line without overcoming unnecessary obstacles brought on by lack of patience and forethought.

Thanks for reading!
 
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MadeByMiller

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That is some pretty country showing in the background of your photos, does it stay that green all summer or turn brown?
Thank you, we absolutely love it here. It depends, at this time last year we were in a drought and the grass was already going dormant. Hopefully it will stay green until fall this year, we've gotten a lot more moisture.

Great job! Now you just need it to snow again so you can play 😆
Many thanks! I'd like to see if I can tune the governor to squeeze even more RPM out of it. It will be fun in the snow, but I've already used it to start fixing my gravel driveway from where the rain has washed it away on the slopes. I also have a load of topsoil coming soon for some projects around the yard.
 
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MadeByMiller

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The first big job around the property for the 1816 is underway! Yesterday we measured out a 30'x30' area we are needing to level off for a swing set that is currently occupying half of my shop (see truckload of boxes) and I mowed the grass down as low as possible.
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A truckload (12 yards) of topsoil showed up today to level off the pad. There's no access point for a dump truck to my backyard, so I had to have it dumped in the driveway. The 1816 handled so well, scooping overflowing buckets with relative ease, and I had the whole load moved in less than an hour! I placed buckets where I thought I would need the dirt, and after cleaning up and raking up the driveway I began roughly grading the pad. Unfortunately, I don't have a laser level/transit so for now I just eyeballed grade.
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Tomorrow I plan on picking up some stakes and string line with bubble level and establishing grade using that. It sure looks like I'll need another load, but I'll know for sure tomorrow. I tried to get another load delivered today but the soonest I can get it will be next week.
 

Boostingaz

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Thank you! Wish I could accelerate this project, really getting annoyed with having my shop full of swing set boxes, but we will probably have to wait a month after I seed the new pad with grass before we can even assemble it and get me my shop back.

Throw a little railroad tie border down, rubber mulch. Done. Get your shop back.

I used 8 tons of rubber mulch under our playset and it is great. Has just the right amount of squish were I can throw them out there and not be worried. I also built a fence into the retaining wall around ours so they are trapped in and can't run away hahaha.


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MadeByMiller

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Throw a little railroad tie border down, rubber mulch. Done. Get your shop back.

I used 8 tons of rubber mulch under our playset and it is great. Has just the right amount of squish were I can throw them out there and not be worried. I also built a fence into the retaining wall around ours so they are trapped in and can't run away hahaha.


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My goodness, that's an amazing setup! My wife and I are drooling over it. Rubber mulch (and wood chips/wood mulch or pea gravel) did cross our minds as a way to accelerate the project. Cost is a big factor, but we are concerned with our littlest ones trying to eat the mulch and the additional work involved keeping it out of the grass surrounding it and maintaining it - we just decided that grass would work best for us. We may be interested in putting sod down to help speed up the project, but I'm not aware of there being a variety out here that doesn't require watering in our dry months here, and watering isn't really something we're wanting to do.
 
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MadeByMiller

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Sunday afternoon I took back the shop! It's looking like it will be a few more weeks minimum before we will have grass that will be ready to put the swing set on, and I'm not willing to wait that long to continue storing these massive boxes in my shop. Testing my Tetris skills, I was somehow able to shove them all into the already packed storage shed. Don't look at how messy the shop is please!
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RickP

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Lifetime brand -- that's who made our shed. I didn't know they made swing sets as well.

I feel your pain on storing those boxes -- they were stacked in our garage for months before I could get the shed foundation completed.

Very nice restoration of your skid loader -- I'll bet you were extremely happy to have that available for grading the swing set area.
 
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MadeByMiller

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Lifetime brand -- that's who made our shed. I didn't know they made swing sets as well.

I feel your pain on storing those boxes -- they were stacked in our garage for months before I could get the shed foundation completed.

Very nice restoration of your skid loader -- I'll bet you were extremely happy to have that available for grading the swing set area.
We did not want a wooden swing set that would require yearly maintenance/staining, so we paid a bit more for the Lifetime set - time will tell if it was worth it.

Thank you! The skid loader is totally awesome, couldn't be happier with it.

Excellent job on the tractor Austin. Turned out fantastic and looks like it's getting some good use already. :thumbup:
Thank you very much Mike! We're so glad to have it.
 
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MadeByMiller

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An update to the swing set pad project! We received our second load of topsoil early last week to finish the level grade and slope off the pad. We decided to purchase this laser to set grade with and I'm glad we did, it's surprisingly high quality for the price point and has some neat features that I hadn't seen on other lasers I've used in the past. I ended up having just enough dirt to make a nice gradual slope off the pad, which required about 20" of fill at the lowest point. Once again, the little 1816 just performed flawlessly - I love this machine! Once the pad was finished I gave it a hand wash with the new pressure washer and foam cannon.
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After deliberating the cost/benefit of sod, hydroseeding, or seed, we decided that seed would be the most cost effective and ultimately best choice for our needs. Rather than source our seed from a big box store, I went to a local landscape supply company that offers a broad selection of grass seed tailored to our region and conditions. They set me up with a resilient, drought resistant grass seed that does not require irrigation once established, as well as starter fertilizer and germination blanket. Having never planted grass seed before I was (and still am) quite nervous about a successful outcome. As suggested by the seller, I raked in the fertilizer after spreading the granules to promote root establishment.
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Then spread the grass seed at approximately 4lbs/1000 sq ft in several even passes with my Scott's spreader.
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Lastly, I staked down the germination blanket and watered.
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Overall it went quite smoothly! We're looking forward to seeing some grass popping through the blanket within the next week.
 
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MadeByMiller

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I'm relieved and excited to report that we have germination! This afternoon I was pleasantly surprised to see thousands of little grass shoots sticking up through the blanket. I promptly grabbed the fancy camera to try to capture the little guys, which was mostly a fail. My neighbors probably got a kick out of seeing me laying down on my belly to get these shots anyways.
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While I was at it, I took some real wannabe photos with an extension tube on my 50mm lens of my wife's iris flowers:
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MadeByMiller

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Today we received a visit from member @Trapps as he makes his way back home from his epic motorcycle road trip. It was really great to meet him and hear stories from his trip as well as share my humble shop. With that being said, my shop was absolutely in no state for visitors just mere days ago, so his visit really gave me the motivation I needed to get it whipped into shape!

Ever since I sold my plasma table last year the shop has been in an awkward state of disorganization, so after I cleaned up my mess from the skid loader overhaul, I started brainstorming and acting on some reorganization. As a reminder, here's what I started with thanks to my negligence...
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We sold the dining table, recycled the cardboard, and moved some junk to the shed. I moved the new cabinets into a position that I think will work well - out of the way for most work, but moveable if I need more room in the area near the overhead door. I moved the TIG welder from the floor to on top of the mid-height cabinet where the red Craftsman box was (said box moved underneath the shop press), and put the ********* and Decker bench grinder on top of the new Lista cabinet. One of the biggest changes is the move of the big Morgan Chicago 360 vise from the stand to the fab table, a move I deliberated over for a bit before bear hugging that beast of cast iron into it's new home.

With everything organized, I did a nice deep clean by blowing off all surfaces with compressed air before vacuuming and wiping things down. Lastly, I mopped the floor twice. Of course I did get distracted many times throughout this process, most notably to clean up the table and base of my variable speed Powermatic drill press:
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And here's the result of all the work described above:
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I'm really happy with the outcome. The shop has never felt so open and streamlined as it does now. There is plenty of room now to pull a vehicle in partially to work on, or just have a large open area for larger projects. There's still much I'd like to do of course, namely a better/more space efficient pressure washer cart, and I'd like to finally get my great grandfather's lathe up on either some original cast iron legs or fab up my own stand for it.
 
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